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Megashift working with a few bugs

Posted: Sat Aug 08, 2015 6:33 am
by Gnx412
Hello everyone name is Joe I am new to the forums and need some assistance. Have a 90 Deville with a 4t65e controlled with a gpio board built as a 4l80e and it works pretty good :D butttt. When I drive aggressive system goes into manual mode by itself. Wires were wired as force automode for now. Also megashift won't let me set rev checking :| I know a datalog is crucial and will try to get one but maybe my description can lead you guys on to a clue thanks!

Re: Megashift working with a few bugs

Posted: Sat Aug 08, 2015 6:57 am
by Bernard Fife
gnx412,

Few things can force manual mode (as opposed to force auto mode, which has a number of settings).

Having either of the shift buttons grounded can do it, even though this may be brief and accidental. The best bet if you want to force auto-mode at all times is to tie the upshift and downshift button leads (Amp 15 and Amp 4) to 5 Volts (such as Vref on Amp 28). As a work-around, you might increase the shift button duration: http://www.msgpio.com/manuals/mshift/V5tune.html#gs under Shift Factors

Sometimes if the shift tables are not identical, accidentally using the wrong table (due to grounding or un-grounding of the 4WD switch lead) can lead to no shifts so that it feels like manual mode.

Having the shift table set up so that shifts would exceed the rpm limits will also feel like manual mode had been engaged.

But it's hard to say anything specific without a datalog and a settings (msq) file.

Lance.

Re: Megashift working with a few bugs

Posted: Sat Aug 08, 2015 8:23 am
by Gnx412
Thanks so much Lance, I will try to get msq, it was definitely in manual mode because the little box at the bottom changed to manual I'm wondering if there is some error in the firmware because it wont let me save the rev checking option, says burned then if I restart tunerstudios it says you have changes that aren't written and I click write to controller until I'm blue and it just wont burn I'm hoping with an msq of the manual mode happening it will show something

Re: Megashift working with a few bugs

Posted: Sun Aug 09, 2015 10:30 am
by Gnx412
Ok so your info was helpful of course and what I can tell you is that I am sure that it is in manual mode because I see the little box on the bottom go from blue auto to green manual when I get frisky with the throttle. I hooked the wires to 5v and it definitely helped by at least going back to auto mode by itself as before when it went into manual it would stay in manual. I finally got a datalog and hope you can see if I'm missing something or if there is an error somewhere. Just to clarify everything is soldered heat shrunk and does work almost seamless when driving normal around town and on the highway and this is my first mega-product I have built. The transmission is from a 01 Pontiac Montana and I had to fabricate axles and modify some mounts to get everything to work and so far success first shot. :mrgreen: I have two logs one is normal driving but the one that has the manual mode problem says too large very frustrated maybe I can email to you?

Re: Megashift working with a few bugs

Posted: Sun Aug 09, 2015 10:40 am
by Gnx412
second try

Re: Megashift working with a few bugs

Posted: Sun Aug 09, 2015 10:42 am
by Bernard Fife
gnx412,

I have asked the forum admin team to increase the file attachment limit from 1 MB to 5 MB per attachment, so you might try re-uploading the log in a little while.

You might also check this post for editing logs to make them shorter: viewtopic.php?f=4&t=1017&p=5500#p5492

One more thing to check when you have problems only under high loads, etc. is that you have very good grounds, as 'iffy' grounds can cause exactly the sort of issues you are seeing.

Lance.

Re: Megashift working with a few bugs

Posted: Sun Aug 09, 2015 11:05 am
by Bernard Fife
gnx412,

It looks from the second log that the downshift button (DWN in the log) has been grounded from 50.390 seconds until 57.219 seconds. Not surprisingly, that provokes manual mode.

The question is if this was an actual grounding of the down button circuit, or something else. One hint is in the aux channel voltage which is a separate circuit. Curiously, it rises from 0.700 Volts to as much as 2.7 Volts during the same time the downshift button is supposedly pressed, and this suggests to me that either the grounds are suspect, or there is an issue on the board somewhere. The downshift button returning to normal appears to coincide with the pressing of the brakes which again suggests a ground or board issue.

There are also a number of VSS resets at the point at which the button shows as grounded.

That doesn't mean that there isn't issues in the code; there may be and I will have a look on my bench. But the above clues, plus the fact that it happen only under specific circumstances (driving aggressively) suggest a wiring or board issue. So while I look closer on my bench, you might want to have a look at your grounds and your board to make sure these are correctly configured. I would start by making sure that the resistance from my board to the battery's negative terminal is 1.0 Ohm or less.

Lance.

Re: Megashift working with a few bugs

Posted: Sun Aug 09, 2015 3:08 pm
by Gnx412
K I checked resistance from pin at board to the body ground that its connected to under dash about.02 The bolt under dash I used is right to the body and .02 ohms. From that bolt various parts of body ground as well .01-.02 ohms. Trans case to batt .002. Again all connections are soldered, ground is an eyeloop soldered. The wiring at trans is wired exactly as its guided in the 4l80e scheme with diodes and resistors close to connector.

Re: Megashift working with a few bugs

Posted: Sun Aug 09, 2015 3:10 pm
by Gnx412
The only other thing I'm wondering is I have a drac box wired into board as another gentleman did is it possible its causing noise

Re: Megashift working with a few bugs

Posted: Mon Aug 10, 2015 5:45 am
by Bernard Fife
gnx412,

It's unlikely the DRAC is causing problems, unless it is defective (which is possible, of course). You could try by-passing it, I suppose.

If this was mine I would also check the grounds for the alternator and engine to the battery, as ground issues there can cause what seem like ground issues in unattached devices.

It may also be that the 12V supply is very noisy (for any number of reasons), and this is causing the issues you see. In that case, you can put a car stereo power filter in the 12V feed to the GPIO board. Normally this is put in place for reset issues, but it can also solve some problems that are significant enough to cause the sort of issue you see, but not quite big enough to cause resets. There is more information here: http://www.megamanual.com/ms2/tune.htm#resets

Did you try increasing the 'shift button duration' setting? You can set it as high as 1000, and that's what I recommend for you.

Lance.